Legit' Motorola 2N4427 found on eBay
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- proppa neck!
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Legit' Motorola 2N4427 found on eBay
Alright necks,
I ordered some of these the other day, they arrived today, & can confirm they're the real deal & not those shiny clones everywhere that are marked "00xx".
These are dated 8435, so manufactured in August 1984.
Motorola ceased production of the 4427 in the 90s, so anything dated 00xx (like clones are) is a fake.
The item # is 233731576578
He sells a long list of new old stock Transistors, so you might find something you want there that's the real deal.
Just thought I'd share & give the heads up, as I've read on here that they're hard to get now.
I ordered some of these the other day, they arrived today, & can confirm they're the real deal & not those shiny clones everywhere that are marked "00xx".
These are dated 8435, so manufactured in August 1984.
Motorola ceased production of the 4427 in the 90s, so anything dated 00xx (like clones are) is a fake.
The item # is 233731576578
He sells a long list of new old stock Transistors, so you might find something you want there that's the real deal.
Just thought I'd share & give the heads up, as I've read on here that they're hard to get now.
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- teckniqs
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Re: Legit' Motorola 2N4427 found on eBay
£2.50 isn't bad at all.
- Bton-FM
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Re: Legit' Motorola 2N4427 found on eBay
The fake ones have a batch number of ‘KO’ followed by 3 numbers. The Chinese 2N4427, ‘5109, ‘3866 are all the same transistor!
If anyone has a good idea for another more modern way of doing the a 1 watt stage that’s cheaper, I’d be interested. I tried the BFG135, but it’s quite hard to squeeze a comfortable Watt out of one.
I’ve got a few others in mind, but the smaller LDMOS devices run at low voltages which is a PITA!
If anyone has a good idea for another more modern way of doing the a 1 watt stage that’s cheaper, I’d be interested. I tried the BFG135, but it’s quite hard to squeeze a comfortable Watt out of one.
I’ve got a few others in mind, but the smaller LDMOS devices run at low voltages which is a PITA!
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Re: Legit' Motorola 2N4427 found on eBay
I've been playing with the RD01MUS2 (not RD01MUS2B which is a totally different part). Like you say it's meant for 7.2V but it runs fine at 12V. Rated VDSS is 40V. I get about 1.2W out of it at 12V direct into a 50R load without any matching. Probably closer to 1W once I add LPF.Bton-FM wrote: ↑Wed Apr 14, 2021 5:20 pm The fake ones have a batch number of ‘KO’ followed by 3 numbers. The Chinese 2N4427, ‘5109, ‘3866 are all the same transistor!
If anyone has a good idea for another more modern way of doing the a 1 watt stage that’s cheaper, I’d be interested. I tried the BFG135, but it’s quite hard to squeeze a comfortable Watt out of one.
I’ve got a few others in mind, but the smaller LDMOS devices run at low voltages which is a PITA!
- Bton-FM
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Re: Legit' Motorola 2N4427 found on eBay
How hot is it getting? Also, how much power are you driving it with?jvok wrote: ↑Sun Apr 18, 2021 11:44 amI've been playing with the RD01MUS2 (not RD01MUS2B which is a totally different part). Like you say it's meant for 7.2V but it runs fine at 12V. Rated VDSS is 40V. I get about 1.2W out of it at 12V direct into a 50R load without any matching. Probably closer to 1W once I add LPF.Bton-FM wrote: ↑Wed Apr 14, 2021 5:20 pm The fake ones have a batch number of ‘KO’ followed by 3 numbers. The Chinese 2N4427, ‘5109, ‘3866 are all the same transistor!
If anyone has a good idea for another more modern way of doing the a 1 watt stage that’s cheaper, I’d be interested. I tried the BFG135, but it’s quite hard to squeeze a comfortable Watt out of one.
I’ve got a few others in mind, but the smaller LDMOS devices run at low voltages which is a PITA!
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Re: Legit' Motorola 2N4427 found on eBay
Not hot enough that I'd worry about it. I soldered the tab down to a solid ground plane which seems to keep it cool (helpfully the tab is the source pin so you can do that). I set the bias for 100mA and just use a diode in contact with the top of the package for temp compensation. With that simple setup bias only drifts by about 5mA between cold and fully warmed up.
Drive power is hard to say yet because I don't have input matching fully worked out. But if you believe the graphs in the datasheet it should be around 20mW. Maybe slightly less because the datasheet numbers are for 520MHz. Gain should be a bit higher on band II.
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Re: Legit' Motorola 2N4427 found on eBay
2n4427 somewhere i saw that 2n4427 work @175 mhz max and another say it go up to 400mhz and here they talk at abt 500
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Re: Legit' Motorola 2N4427 found on eBay
The RD01MUS2 is a cracking little beast! I found that I could run it at (pretty much) a Watt out with just a Colpitts oscillator driving it. I used a 7808 to run the two stages, and have a lowpass Soshin filter after it. It makes for a really tiny, two-stage exciter!
The second version I tried uses a pseudo-Kallitron two-transistor oscillator using a couple of surface-mounted FETs (like 2n4416). This gives the advantage of isolating the modulator more from the 1 Watt stage and so less prone to hum. The PCB (hand etched, using marker pen resist) including a PLL using an SM PIC and a SM 145170 ended up being just 5 X 2 cm! I used SM moulded chokes for the coils, and spent nearly 45 minutes trying to find the last 22p NPO SM cap I had when I fired it across the office from the tweezers! When I get this cracked, I'll work out a small housing for it, and get it made in the Far East for next to nothing.
The second version I tried uses a pseudo-Kallitron two-transistor oscillator using a couple of surface-mounted FETs (like 2n4416). This gives the advantage of isolating the modulator more from the 1 Watt stage and so less prone to hum. The PCB (hand etched, using marker pen resist) including a PLL using an SM PIC and a SM 145170 ended up being just 5 X 2 cm! I used SM moulded chokes for the coils, and spent nearly 45 minutes trying to find the last 22p NPO SM cap I had when I fired it across the office from the tweezers! When I get this cracked, I'll work out a small housing for it, and get it made in the Far East for next to nothing.
"Why is my rig humming?"
"Because it doesn't know the words!"
"Because it doesn't know the words!"

- reverend
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Re: Legit' Motorola 2N4427 found on eBay
Those Soshin filters claim an insertion loss of 3 dB - don't they get mighty hot with 1 Watt running through them?
if it ain't broke, keep tweaking
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Re: Legit' Motorola 2N4427 found on eBay
I haven't seen 3dB loss through them. Measured here, I lose 1.5dB @98.4MHz, with the unfiltered input at 1121mW (30.5dBm), giving a net output power of ~29dBm at 805mW, and no measurable harmonic content at all. There's also no heat to mention.
I'm experimenting with a rather cunning tracking harmonic filter in an effort to get a truly monotonic 1 Watt VCO out of a tiny PCB in a copper-clad box. Early results are promising, and when I (finally) get home, I'm going to do some serious work on this. I can envisage a cheap commercial module with a built-in PLL, which will be one-time programmable to a specific frequency. (I think that frequency agility is really somewhat over-rated!).
Now that the bigger FETs are getting cheaper, and the broadband circuits are now well-known, good rigs will be getting cheap to build again! The most expensive parts will be the power supplies and the heatsinks!
I'm experimenting with a rather cunning tracking harmonic filter in an effort to get a truly monotonic 1 Watt VCO out of a tiny PCB in a copper-clad box. Early results are promising, and when I (finally) get home, I'm going to do some serious work on this. I can envisage a cheap commercial module with a built-in PLL, which will be one-time programmable to a specific frequency. (I think that frequency agility is really somewhat over-rated!).
Now that the bigger FETs are getting cheaper, and the broadband circuits are now well-known, good rigs will be getting cheap to build again! The most expensive parts will be the power supplies and the heatsinks!
"Why is my rig humming?"
"Because it doesn't know the words!"
"Because it doesn't know the words!"

- Bton-FM
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Re: Legit' Motorola 2N4427 found on eBay
@Albert H
Are you using varicaps in your filter elements for the tracking?
Also, is the Oscillator affected much by changes of the loading of the RD01MUS2 since there is no buffer? Since the RD01 is MOSFET the OLPD switching could be done by pulling the bias down I ground. Is this how you’ve implemented OLPD?
Is there a benefit of running the RD01 at a lower voltage?
Did you use those coilcraft moulded coils? I saw them a while ago but they seem very expensive for what they are.
Are you using varicaps in your filter elements for the tracking?
Also, is the Oscillator affected much by changes of the loading of the RD01MUS2 since there is no buffer? Since the RD01 is MOSFET the OLPD switching could be done by pulling the bias down I ground. Is this how you’ve implemented OLPD?
Is there a benefit of running the RD01 at a lower voltage?
Did you use those coilcraft moulded coils? I saw them a while ago but they seem very expensive for what they are.
- thewisepranker
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Re: Legit' Motorola 2N4427 found on eBay
So now the cloners are going to mark those BC108s with 8436 instead of 00xx, happy days!
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Re: Legit' Motorola 2N4427 found on eBay
No. It's a high speed power op-amp configured as a voltage tunable filter.
Not at all. The output from the VCO is from the low impedance point (and purest output) from the emitter of the oscillator transistor (or the source in the FET version). OLPD just grounds the drive at the gate of the FET - it's crude, but there's no significant leakage,
Yes. It runs much colder. You don't get as much gain or power out, but it doesn't matter much. The difference is just a few mW.
I used something similar from a manufacturer in Shenzhen. They're not too shabby, and a lot cheaper.
"Why is my rig humming?"
"Because it doesn't know the words!"
"Because it doesn't know the words!"
